The pleasure of getting it wrong… so many times
My wing joiner was bent, and so I ordered a 7mm silver steel rod to replace it, on arrival I cut it to length, bevelled the ends and polished it with some polishing paste I had lying around. It looked perfect so I popped it into the wing, and discovered it was a little restrictive, not deterred I kept going, twisting it back and forth while shoving it in. At some point the resistance got beyond a joke and I quickly retreated, after a little bit of wrangling and some very sore fingers I got it out.
My beautifully polished rod was now scored, so I went back and polished it up again, a trial fit of the bent rod into the tube was fine, so I figured I must have caught a little bit of swarf on my last attempt so I proceeded without caution, it felt a little smoother and then all of a sudden it locked up. I could maybe budge it 5º this way and that but no more, I wiggled it back and forth whilst the rod was clamping in a vice, it was slow progress and after fifteen minutes I decided to put a tape marker against the edge so I could see how much progress I was actually making extracting the rod, five minutes later the tape had not budged even a fraction of a mm.
I considered my options, but it basically came down to one, twist the wing beyond the 5º of play and see what happens, I figured I would either break the wing, the rod would come free, or I would extract the rod with the glued in aluminium tube. There was a reassuringly frightening crack and out came the rod with the tube.
To free the rod from the tube I drilled a 7mm hole in a piece of MDF, which took the rod but stopped at the 8mm diameter tube, with a slimmer bit of steel rod down the tube I hammered it out, progress was good and both rod and tube punched their way through the MDF without parting company! I repeated the process with a hole in a lump of beach and thankfully that did the trick.
Googling to find 8mm aluminium tubing with a 0.5 wall thickness was not encouraging, so I thought I’d have to try and fix the original tubing, this involved lots of attempts to polish the inside, by putting the steel rod in a drill, liberally dousing the inside of the tube with polishing paste, and with the drill running I slid on the tube, in hindsight this might have ended in injury, but luckily not on this occasion. You could not ask for a better fit, it was really smooth. So I cleaned it all up did a trial fit and managed to lock the two together again, this happened several times, what was in Einstein said about repeating the same thing and expecting a different outcome?
Fortunately I alighted upon some 8mm tube with a 0.45mm wall thickness, and eagerly anticipated the delivery. The rod fitted the tube perfectly, all that was left was to cut it to length pop it back into the wing and I would be well on my way to repairing the wing.
It was when dry fitting the new tube that I discovered I’m a slow learner. It appears the new tube was reluctant to slide in where the old tube had been, and I was again stuck with a bit of metal well and truly jammed and sticking out of the wing! Eventually I managed to extract it and decided to see if I could free up the holes through the ribs by putting the spare bit of tube, with sharpened end, in a hand drill and whilst spinning the tube I was able to feel my way through, success! In with the pre-cut length and it jammed again, my sense of humour for this project was bordering on failing at this point. After some barbaric practices I was able to extract the tube and I decided to cut my losses. I went back to the off-cut which was over length and putting it back in the drill. I spun the tube into place with copious amounts of CA, and then cut it flush… Done!
The balsa wood repairs went okay, so it's just a little tidying up to do and I think I'm ready to recover the wing.
Any thoughts on using 4mm carbon tube for the pins that secure the leading edge into the fuselage?